It's not impossible that there could have been a freeze up of the regulators on the Interspiro (AGA) masks, but unlikely, they perform well in extreme cold environments. Most likely a cold water failure would be the first stage.John C. Ratliff:I find it interesting that they were using FFM, that the air in BM Duque's tank was completely depleted, and that LT Hill's tank had only 90 psig in it. The air tested good. There was no CO, ethanol, or screened drug in either diver's systems.
While these findings of fact are interesting, I don't think they pinpoint the exact cause of these two fatalities. A thorough "Fault Tree Analyses" would be appropriate for this event, which is a Systems Safety methodology of looking at an accident scenario. I may do this a bit later, and post some of it here. But one observation is that with a FFM, divers rarely die of anoxia using air with scuba. Something had to cause them to loose their air supply.
Since this is the ScubaBoard, I have to ask if anyone has experience with AGA Full Face Mask a few questions. I find it curious that these divers were very quickly out-of-air at depth, probably because they had been working extremely hard trying to swim to the surface while greatly overweighted, and in extremely cold (29 degrees F) water. I know that the AGA mask has a positive pressure breathing feature on it too (or at least used to in the 1990s). My question to those familiar with the mask (I've only used it a few times, and in a pool) is this, under extreme workload, with high demand for air in extremely cold water, is the AGA FFM prone to icing-caused free flow? If so, and that happened in a positive pressure mode, how long would it take to drain a 100 cubic foot tank, assuming a break in the seal around the face, at a depth of greater than 150 fsw?
John C. Ratliff (SeaRat), CSP
Extrapolating from the report, the dive was approximately 38 minutes from the start of the dive to the recovery of the divers, with some breaks in between for the issues stated. However, keep in mind, that when you don a full face mask, you are breathing from your tank unless you're using an ambient breathing valve. My understanding is that these were gray rubber masks, and I don't think they were fitted with ABV's. I'll try to find out. Add to this dive time, at least several minutes (6 minutes at ice edge) of surface time while breathing from the tank, the additional exertion from over weighting, the available air is being consumed. I don't know and it's not stated if the masks were positive pressure or demand regs. I can find this out as well. In the investigation of the equipment, the masks were determined to be in proper functioning condition. The missing protective guard on the regulator is the Shield Ring. This would have no adverse affect on the function of the regulator.
Not knowing at what stage in the dive that the divers made the uncontrolled descent, assuming that it may have been with the rapid payout of line early in the dive, a single 100 cf bottle with an unknown quantity of gas, isn't going to last long at depths in excess of 180 feet, especially with the extreme workload and onset of panic. This is an assumption, but I don't think it's a far stretch.
I would have a significant concern of the fit of the mask, with the hood being fitted over the mask straps. Assuming they were wearing neoprene hoods not properly trimmed for the masks in the first place, then follow-up adjustments would be almost impossible, especially with heavy gloved hands and limited dexterity due to exposure. Pulling the hood over the straps is often an attempt to get the masks to seal directly to the face when the hood isn't trimmed to fit with the mask over the hood. This limits access to the tag end of the straps for adjustment and can interfere with the buckles. It is possible that they could have had fit issues causing leaking of air out of the masks, but this would be jumping to conclusion. Small or narrow faces can be difficult to fit without the interference of an ill fitted and improperly donned hood.
As stated in the report, there was an accumulation of many factors that caused this accident. It appears that with these findings, the directives issued by Adm. Allen are sound and should go a very long way to preventing similar incidents in the future.