Sonic04GT
Contributor
Awesome. Maybe I will check that later. I want to say I remember doing that in the past. Thank you again!
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Just to add to this sage advice, I once had an odd acting Atomic and when I opened it up I found the nylon part, they call it the orifice sleeve, cracked so the action of the wave washer was inhibited. Judging by the time it took to get that part I don’t think this happened very often but it is something to look for when and Atomic behaves oddly.I hate to rain on this parade, but let me add a bit of caution here. Folks that were helpfully teaching this diver how to eliminate his freeflow only addressed half the problem. And in doing so, they potentially made things less safe for this diver.
I note that instructions were given to adjust 1/16 to 1/8 of a turn, which is correct, if it's just a poppet contact issue.
Yet the diver felt it necessary to screw in a full 1/4 turn - two to four times what was recommended.
Nobody spoke to the drop in lever height that is caused by overtightening the orifice. With a low lever, gas flow at depth can be severely compromised. Changes in these toys occur with very little adjustment.
I'm not saying that reg service is rocket science. And as a frequent DIY poster on this Board, I obviously don't think everything needs to go to a shop. Frankly, I'm afraid of a lot of young shop techs. But it's taken me a long time to learn all the tricks, and I don't think y'all did this diver a favor by suggesting that it's as simple as 1/4 turn on the orifice.
And there was also the comment about pressure on the knob causing freeflow.
Atomics are the very best second stages on the market today, IMO. The problem described, especially requiring a full 1/4 turn to fix, is odd coming right out of service. Odds are it was just a sloppy tuning job. But this is a big enough discrepancy that I'd say, "take it back to the shop and take it apart". Odds are, it'll go right back together with a proper tune.
But maybe the seat wasn't pushed in flat. Maybe the tiny spring that creates the seat saver was omitted. It's possible that this isn't just a tuning problem, and if this were my reg right after I'd serviced it, I'd take it apart and do it again.
@Sonic04GT , come join us in the DIY Forum! There's lots to learn, and it's fun doing it yourself. But be careful at the beginning.
Sermon over...